FIT Service Specialty: Improving Control Systems
Introduction
FIT provides process control system audit services to clients who want to
assess the overall capabilities of their control systems and how well they are
used by plant personnel. The primary objectives of the audit are to identify
areas for improvement in control system performance and to determine the
cost/benefit details of system upgrades and new applications.
The field of process control combines the multiple disciplines of chemical,
process, electrical, electronics, computer and network engineering. Control
systems today employ a wide variety of field instrument devices, analysers,
analog and digital controllers, control valves and interconnecting signal
tubing, wiring and networks. Control engineers who are involved in day-to-day
operation and maintenance of control systems must be intimately familiar with
many of these disciplines in order to be effective. FIT audits can provide
valuable insights to these engineers and their managers and assist them in
making quality decisions about the future maintenance and development
activities they should consider for their control systems.
Scope of Work Involved
FIT Consultants assist clients by providing a comprehensive audit that comprises:
- Determination of the current status of the control systems at all levels.
The levels may include:
- Field instruments and process analyzers
- Control valves
- Analog and digital control hardware and software at the regulatory level
- Digital control hardware and software at the supervisory and advanced level
- Emergency shutdown sensors and Programmable Logic Controllers (PLC)
- Fire and gas detectors and alarm hardware
- Signal tubing, wiring and networks
- Control rooms and ergonomics
- Determination of the current organization of control systems group,
engineering department and instrument/electrical maintenance department. The
organization includes the local plant and any head office support staff plus
outsourced services.
- Comparison of the current status with "Best Practices" in the
industry in order to determine opportunities for improvement.
- Determination of activities and projects to be carried out to reach
"Best Practices". The activities and projects include updates to
control systems at all levels as well as organizational improvements.
- Determination of preliminary cost estimates and the
economic benefits of control system and control room upgrades. A proposed plan
of action with time lines and major milestones is prepared.
Methodology
The methodology comprises three phases:
- Information gathering - Before coming on-site with a compact team of
seasoned control system consultants, FIT will transmit a "request for
information" to the client. Some of the requested data includes
organization charts, Process and Instrument Diagrams (P&ID), Simplified
Process Flow Diagrams (SFP), and local plant economics information. After
arriving on site, the team
will conduct a number of interviews that includes plant personnel at the
management level, process control group, operators in the control room(s) and
the field, plus instrument and electrical maintenance personnel. Sometimes it
is necessary to interview some people from the information systems department
depending on how a plant is organized. FIT uses interview templates that
improve the effectiveness of the information gathering process.
- Information analysis - After the information gathering process has been
completed on-site, the FIT consultants will frequently return to their home
bases and begin the analysis activity. It is also possible to do the analyses
at the client's location if desired. The analysis phase begins with a review
of the interview notes and preparation of a list of follow-up questions that
the client needs to respond to. Once all the clarifications have been
received, the analysis phase will be completed. A key activity is the
development of the opportunities via the "Gap Analysis" by comparing
"Best Practices" in the industry with the observed practices at the
client's plant. Considerable attention will be paid to local work practices, skill
levels, and availability of resources because FIT knows that it is very
important to reflect
the client's circumstances while still trying to achieve "Best
practices" in the long term. The deliverables from this phase include:
- A proposed set of activities and projects that should be considered over a
five year period
- A feasible time line or implementation schedule of the proposed projects
- A preliminary estimate of the potential benefits of control system
upgrades or replacements using local economic data
- A preliminary estimate of the project costs using
local resources where possible
- Management presentation - The findings,
recommendations, benefits and costs are packaged on CDROM and presented to the
client on site by FIT consultants and discussed thoroughly. Any changes that
need to be made to the recommendations as a result of the discussions will be
incorporated on a new CDROM.
Examples of Typical Recommendations
Below are some typical examples of recommendations that were made to
clients over the past fifteen years. It shows that wide variety of technical
content is covered in the control system audit:
- Off sites
- Tank farm does not have enough Motor Operated Valves (MOV) to allow
automatic oil movements to take place. Additional MOVs must be installed
over the next three years and a simple oil movement system should be considered.
- Enraf tank gauges are failing frequently and Man Machine Interface
(MMI) is old. Newest release of the tank gauges and a new MMI should be
considered for next year's budget cycle. In addition, a suitable serial
data link should be added to connect the tank gauging system to the
Distributed Control System (DCS) in control room X.
- pH control system in the bug plant should be
replaced immediately.
- On sites
- Regulatory control systems (both analog and digital) are running with 40%
of automatic controllers set to manual. This situation is
abnormal and the reasons for operating the loops on manual must be
investigated in detail and corrected immediately. Not doing so may
result in seriously unsafe process conditions as well as loss of revenue
through poor product quality control.
- Large number of analog and digital loops do not appear to be tuned
properly. Current technology exists to track loop performance
automatically and to propose better tuning constants. This technology
should be acquired and evaluated.
- Several Advanced Process Control schemes have service factors below 60%,
while some are turned off. The causes of these low service factors must
be investigated and the disabled APC schemes turned back on. The
problems with APC schemes are frequently due to poor tuning of regulatory
control loops as noted above.
- There are not enough flow meters on a number of process units to allow
calculation of a material balance. This situation should be corrected at
the earliest opportunity. Current practice is to have an hourly mass
balance that is computed on line using reconciled flow measurements.
- Control valves in several locations do not have positioners. This
leads to very poor loop behavior in most cases. Positioners must be
fitted immediately.
- The instrument air is saturated with water
throughout most of the plant. This is caused by a failed regeneration
control scheme on the desiccant beds of the air dryers. The condition of the
desiccant is unknown. At the very least, the regeneration controls must be
recommissioned.
- Utility Plant
- Insufficient field instruments have led to a situation where the plant
does not know accurately how much steam is provided to each process
unit. Additional flow meters must be installed during the next major
boiler #6 and #7 shutdown.
- The automatic blow down systems do not function
properly. New conductivity analyzers should be installed. This activity can
be carried out during the next planned shutdown.
- Control Rooms
- Utility plant control room is extremely close to a main high pressure
steam header (in fact, it runs partly through the room). This can lead
to unsafe situations in case of emergency. Also, the noise level in the
control room is above the OSHA limit. This control room should be relocated.
Where possible, the consoles should be placed so that the operator
faces the process he controls.
- The console layouts and poor lighting in control
rooms A, B, and C lead to higher than normal operator fatigue and error
rates. These control rooms should be immediately upgraded to current
standards.
- Organization
- Several process analyzers do not work reliably and have poor service
factors. The analyzer maintenance group work load and skill level must
be reviewed and corrections made to improve analyzer service factors.
- There is a lack of clear documentation about emergency shutdown procedures
in the control rooms. These documents should be updated to make them
clearer and possibly be made available on line on the operator console screens.
- Too many nuisance alarms are generated during upsets. Alarms should
be reviewed regularly and rationalized to reduce the nuisance factor to a
reasonable level. New alarm display technology should also be considered
for the next budget cycle.
- Control valve maintenance is outsourced to a local
contractor. There are signs that this contractor is cutting corners and
that valve seats and packing need to be replaced more often than
necessary. A new contractor should be hired, or the service should be
done by the plant mechanics as was the practice about seven years ago.
- There are not enough control engineers to keep the
systems in the plant properly tuned and maintained. There is enough work to
keep two new control engineers busy. Any projects for control systems are
handled by the engineering division of the plant in city Y. The current
complement of engineers and the new ones should be enough to absorb any new
projects, provided that they are handled by engineering division
personnel.